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Toilet Bowl #9295
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Hi @albert21martins |
Hi Bresch, closing |
Bug Report
Hi,
We have a 5 kg coaxial octocopter running with Pixhawk 2.1, Here Gps and version 1.7.3 stable.
We are experiencing some toilet bowl behavior in Position mode. Last week was running everything excellent, than we had a small crash, related to takeoff ramp, and since then, the copter is experiencing toilet bowls and fly aways.
We are getting no error, but after switching back from position to alti the copter is drifting and flying away. We tried to minimize the cable and the components, re calibrated a lot of times and noting.
here one of the logs. May be is it helpful
https://logs.px4.io/plot_app?log=20d49b5c-de94-4186-95b4-dd74c27b3bc5
Thanks in advance,
Albert
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